nutzboutbikes
30-06-15, 08:38 PM
I just wanted to post my finding's and so that it may help other Curvy owners trying to diagnose the same problem I had.
The story, my bike has felt like it has been lacking/bogging at little to part throttle for while and after doing a track day at Snetterton yesterday I thought some thing has to be done, so today I headed out to the bike and was determined to get to the bottom of it!.
I thought it has to be a fuel/carb problem by the way the bike felt so firstly I checked for leaks and none were found, next set the a/f screws dead on 2 1/2 outs as per Haynes and what I had also read on the internet, next up balanced the carbs did this and thought that sounds better so started buttoning her back up, as the air box went back on I thought that sounds bad again so out of curiosity I would just check to make sure all was good with the work I had just carried out, to my surprise I found that when the air box is refitted the air flow to the back carb changes and the carbtune showed it to increase!! :confused:, I had no idea why and still can't figure it out but ah ha I thought gotcha could this be the problem?.
It was at this point I remembered I had posted on a thread just the other day the front carb a/f screw was set at 1/4 of a turn out when I removed them for cleaning, so my next step was to wind the front a/f screw in to 1/2 a turn I allowed 1/4 of a turn for the slip exhaust and when I started her up she sounded sweet again the problem sorted, at last!. :grin:
The story, my bike has felt like it has been lacking/bogging at little to part throttle for while and after doing a track day at Snetterton yesterday I thought some thing has to be done, so today I headed out to the bike and was determined to get to the bottom of it!.
I thought it has to be a fuel/carb problem by the way the bike felt so firstly I checked for leaks and none were found, next set the a/f screws dead on 2 1/2 outs as per Haynes and what I had also read on the internet, next up balanced the carbs did this and thought that sounds better so started buttoning her back up, as the air box went back on I thought that sounds bad again so out of curiosity I would just check to make sure all was good with the work I had just carried out, to my surprise I found that when the air box is refitted the air flow to the back carb changes and the carbtune showed it to increase!! :confused:, I had no idea why and still can't figure it out but ah ha I thought gotcha could this be the problem?.
It was at this point I remembered I had posted on a thread just the other day the front carb a/f screw was set at 1/4 of a turn out when I removed them for cleaning, so my next step was to wind the front a/f screw in to 1/2 a turn I allowed 1/4 of a turn for the slip exhaust and when I started her up she sounded sweet again the problem sorted, at last!. :grin: